DETAIL KOLEKSI

Surveillance, monitoring, dan analisis produksi untuk meperkirakan kinerja injeksi air zona 600 blok "Y" di lapangan "X"


Oleh : Sarah Mandasari

Info Katalog

Nomor Panggil : 326/TP/2016

Penerbit : FTKE - Usakti

Kota Terbit : Jakarta

Tahun Terbit : 2016

Pembimbing 1 : R. S. Trijana Kartoatmodjo

Subyek : Enchanced oil recovery;Petroleum engineering;Reservoirs engineering

Kata Kunci : production, surveillance, waterflood perfomance

Status Posting : Published

Status : Lengkap


File Repositori
No. Nama File Hal. Link
1. 2016_TA_TM_07112207_Halaman-Judul.pdf
2. 2016_TA_TM_07112207_Bab-1.pdf
3. 2016_TA_TM_07112207_Bab-2.pdf
4. 2016_TA_TM_07112207_Bab-3.pdf
5. 2016_TA_TM_07112207_Bab-4.pdf
6. 2016_TA_TM_07112207_Bab-5.pdf
7. 2016_TA_TM_07112207_Bab-6.pdf
8. 2016_TA_TM_07112207_Daftar-Pustaka.pdf
9. 2016_TA_TM_07112207_Lampiran.pdf

T Tugas akhir berjudul “Surveillance, Monitoring, dan Analisis ProduksiUntuk Memperkirakan Kinerja Injeksi Air Zona 600 Blok Y di Lapangan X”membahas tingkat keberhasilan waterflood. Analisis tersebut diharapkan dapatmemberikan masukan untuk project waterflood yang akan datang.Analisis menggunakan software DSS yang memperlihatkan productionperformance Zona 600 Blok “Y” terjadi peningkatan produksi sebesar 531,941BBL setelah dilakukan waterflood. Analisis DSS tentang respon dan konektivitasmemperlihatkan 10 pasangan sumur injeksi dan sumur produksi terkoneksidengan baik. Analisis DSS tentang Voidage Replacement Ratio (VRR) yaitu 0.65yang berarti injeksi yang dilakukan belum optimal. Analisis DSS tentang bubblemap memperlihatkan jari–jari pengurasan yang bernilai lebih dari 150 m terdapatdi dua sumur produksi yaitu sumur R029 dan R032HZ. Analisis DSS tentangscatter plot menunjukkan empat sumur produksi dengan water cut di atas 70%selebihnya masih di bawah 70%. Analisis DSS tentang Hall plot terlihat satusumur injeksi mengalami plugging, dua sumur terindikasi terdapat fracture, dandua sumur lainnya normal atau stabil. Diagnostic plot memperlihatkan enam darisembilan sumur produksi mengalami channeling air injeksi.Analisis modifikasi Buckley–Leverett menurut Welge memperlihatkanbahwa waktu breakthrough selama 601 hari atau 1.6 tahun dan total kumulatifproduksi 1,746,524 STB yang berarti Recovery Factor waterflood sebesar 43%.

F Final project titled "Surveillance, Monitoring, and Production Analysis toEstimate Waterflood Performance of Zone 600 Block Y at Field X" discusses thesuccess of waterflood. The analysis is expected to provide idea for the upcomingwaterflood project.Analysis using DSS software shows that the production performance ofZone "Y" Block 600 has an incremental production of 531.941 BBL. The DSSanalysis on the response and connectivity among the injection and the productionwell shows that ten pair of injection wells and production wells are connectedproperly. The DSS analysis of Voidage Replacement Ratio (VRR) is 0.65, whichmeans the waterflood of Zone 600 Block "Y" is not optimal yet. The DSS analysisof the bubble map shows that the drainage radius of more than 150 meters are foundin two production wells, namely R029 and R032HZ. The DSS analysis of the scatterplot shows that the water cuts of four production wells are above 70% and the restof the wells are still below 70%. The analysis of DSS on Hall plot shows that oneinjection well experiences plugging, two wells are indicated the presence offracture, and the other two wells are considered normal or stable water injection.Diagnostic plot shows that six of nine production wells have channeling waterinjection.The analysis of modification Buckley-Leverett of Welge shows that thewater breakthrough time of 601 days or 1.6 years and the cumulative oil productionof 1,746,524 STB which means waterflood recovery factor is 43%.

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